Plastic Fantastic 2

time to fix on the to-do list
anti-roll bar touches the coilovers...
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there is a kit that I hoped would fix the problem... it did but it also required bending the sway bar
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heating
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and before people get persnickety, I know - I don't care, eventually I'll replace with race pieces, but keep in mind that I heated the rear sway bar in the '40 and it's still working just fine

next up, dash lights went out and cooling fan didn't come on.... separated those circuits with this
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new starter, let the smoke out.edited Time for a call to Summit tomorrow because that isn't 6 months old
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thankfully, I have another that works - just needed the bolt retightened - which is what got it pulled.... I probably loosened the wrong nut ah well, works fine now
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and now it's a 1976 Corvette with a 390 hp 427.... the only one... but the badge says so, so, it must be... now it's on the internet so it's doubly true
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headlight wiring
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headlight up
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no headlight
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low beams
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​​​​​​​still working on the bottom stop.edited I'd like it to be adjustable but not quite sure how is the best way to effect that...edited
 
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Just want to say, this is one of my favorite builds. You have provided a lot of informative information. Thanks for taking the time to post your updates.
 
so what happens to the sway bar it becomes more rigid? dont they recurve leaf springs, isn't that the same spring steel?

your work is awesome
 
Had a nice chat with Randy Probst, the guy whose comment started the entire Camaro suspension.edited He's supposed to be here this weekend, might go say hi.edited He was very enthusiastic about it - though, I think he's enthusiastic about anything fast-car.
in other news, circling back to finish things.edited In this case, light actuation
the most obvious problem.... actuator goes too far
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other problem, they can rattle when closed
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edited
the fix is coming but the start of it was tonight

also the missing door rod showed up
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it does have locks, just not key locks on the outside
 
so what happens to the sway bar it becomes more rigid? dont they recurve leaf springs, isn't that the same spring steel?

your work is awesome

yes but they also retemper them in huge furnaces. The issue is if it flexes where you got it red, it could crack. Which is why I did it in a bend - odds are good that any force will take the path of least resistance and bend along the long straight that is between the body bushings.... but let me be sure and underscore this... it's not best practice, but in what I do, it works fine.... after all, it will be a cold day in LA before I spend money for either custom bars or aftermarket bars when I don't know, yet, whether or not these are right for this application. Both front and rear are designed for a 4000 lbs and 5000 lb car - while I suspect the rear will be fine, the front will eventually get a fancy, adjustable race bar..... but I'm way too cheap to buy 2 adjustable bars (or more)
 
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worked on the headlights tonight... I'm going backwards a bit - I'm going to use the original lift mechanism then add actuators.... think it will work better
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whats the part that aways breaks up there? is it the actuator or the mount? seems to me i had to be really creative with jbweld and rivets on one of those pieces on my headlights where it broke in two
 
usually it's a failure of the vacuum system... in this case, I have no vacuum so it wasn't even an option
figured out the distributor problem, a wire got caught between the base and the intake....edited
I see a bit lean, late timing....edited
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what is 'stock'edited
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I'm going back to it for the following reasons
1) there is nothing holding the lower row of rockers in line
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2) note the alignment of the exhaust
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3) doesn't fit well
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I needed to also adjust the rockers - some were way out, but that's to be expected on a new motor....edited
 
I'm not as technical as a lot of you here, but I do like trying to solve problems. For your actuator limiting, if you can't move the limit switches, could you put the base of the actuator on a floating bracket with a spring. Have 2 pieces of metal, 1 rigid mounted and 1 floating held in place with a guide and a spring to pull when it reaches full bottom. When it goes full up the spring would decompress.

Or use like a drawer slide that will allow enough travel of the actuator "extra travel". For example, if the actuator has 10" travel and you only need 6", have a slide that will travel 4".
 
I'm not as technical as a lot of you here, but I do like trying to solve problems. For your actuator limiting, if you can't move the limit switches, could you put the base of the actuator on a floating bracket with a spring. Have 2 pieces of metal, 1 rigid mounted and 1 floating held in place with a guide and a spring to pull when it reaches full bottom. When it goes full up the spring would decompress.

Or use like a drawer slide that will allow enough travel of the actuator "extra travel". For example, if the actuator has 10" travel and you only need 6", have a slide that will travel 4".

good thinking, it's how GM solved the problem - basically, my thought is remove the vacuum actuators and replace the with linear ones. The ratio is even about what you suggestion. the distance to lift the headlight with the pictured parts below is 9 1/2", with these parts, it's 3" and has springs to do what you suggest

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anyway
tonight was blowing warranties
first, I need to start looking at cutting off the anti-chatter from the new pads
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then decide how to mount these
but first, take them apart
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onto boring stuff....edited
shifter boot
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new post covers
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the problem is the top corner wears out and looks terrible
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no idea how this happened... annoying, but not changing it for now
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door panels are coming soon.edited I spent the balance of the evening tuning.... something is off - the IAC is wide open, maybe stuck, dunno... also 10 psi hot oil pressure at idle is not making me happy.... 60 psi at full song, but the low pressure....edited
 
I've said it before, and I'll say it again with illustration.edited The IAC isn't working, so today I called FiTech - they picked up their phone before it rang, answered the question and I have a couple things to do .... and bob's my uncle (well, he was but he died)...

There isn't an aftermarket EFI which works perfect out of the box.I've dealt with all of them now, but that 'doesn't even ring' before their tech line is there to answer my question should be the first thing anyone does when they do EFI.
 
and now, taking it further apart - but with new seat belts
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took a bit of modification to fit

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camera battery died, but the next picture would have shown the dash completely removed
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the power windows weren't getting power.edited The short version, I now know where that orange wire with the red plug goes.... of course, I had nicely tucked it up in the dash about the same level as the headlight switch - which meant pulling it all apart.edited Ah well, they work now





I'm putting the footwell carpet in my car right now. Yours looks like it fits a lot better. Any tips? Glue? Heat gun?



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and now, taking it further apart - but with new seat belts
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took a bit of modification to fit

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camera battery died, but the next picture would have shown the dash completely removed
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the power windows weren't getting power.edited The short version, I now know where that orange wire with the red plug goes.... of course, I had nicely tucked it up in the dash about the same level as the headlight switch - which meant pulling it all apart.edited Ah well, they work now





I'm putting the footwell carpet in my car right now. Yours looks like it fits a lot better. Any tips? Glue? Heat gun?



.

I reused the front two carpets.... the stuff behind the seats is a cheap carpet that is contact-cemented to the various spaces. The area behind the cage is a carpet made of RV carpet insulation and (again) cheap (low weight) carpet. I love german weave carpets, but there was no chance I was using it here because it is really hard to work with - requiring cutting, gluing and a lot of steam.
 
still not 100% on the motor, but the spark plug boots (despite wrap and heat boots) are not surviving well...edited
first replace the IAC valve (it was stuck), then reprogram
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but onto other things. I'm going away from the actuator to C5 headlight motors.edited The biggest issue is opening them if something fails, using the C5 motors makes it possible to open them manually...edited
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still haven't decided if I'll use a C4 controller or Arduino... strangely enough, it would probably be easier to learn Arduino then the wiring for the C4 controller... time will tell
also rebuild the arms
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depin the motors
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in other bench-clearing news, rubber bumpers were installed
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